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So 3 days ago the LEAD 1010 I have was working fine. Then yesterday I try and Home the machine and the button on the interface doesn't do...
IDK maybe the wheels do need replacing? Do you guys have a picture of a worn wheel to show us what that looks like? Sounds like I am not getting...
I will try that out.
Well Im on my 3rd trip of taking this x axis gantry, c beam, etc. apart and here are the problem I keep running into, I have to tighten the...
I did some more pockets and it does in fact chatter on all sides. So I grabbed the bottom of the router and tried to move it and it has slop...
update 17,000RPM Depth 0.25" step over 0.05" conventional cutting 120 feed rate = Zero problems 100 feed rate = Zero problems 90 feed rate =...
Ok so why didn't it happen when I just did a pocket using conventional cutting and not climb cutting?
So here is my setup. 17,000RPM 120 feed rate Depth 0.25" step over 0.05" I used conventional cutting like you asked me to and it worked...
17,000RPM 120 feed rate Depth 0.125" step over 0.05" climb milling Why is happening in only one direction?
1/4in end mill spiral Upcut Is it secured? Yes with 4 clamps.
Why does my Lead 1010 keep doing this? Every time I try and make a pocket using a upcut end mill the machine chatters and vibrates bad when...
I was just checking one of my stepper motors I got from you guys and noticed the shaft can move back and forth in and out of the body. Is that...
Figured it out It's a damaged molex on the end of a AUX cord from Interface to Black Box. I must of messed it up at some point screwing around....
Started having problems yesterday. Running a facing operation to flatten some wood and it keeps stopping randomly. I can run the machine with the...
I had the same problem here and what fixed it was Tramming and using spiral down cut bits. The step over for that would be something like 0.05"...
So I think I got it sorted. It's looking like the MDF spoil board is bowed. And when set up to Face to remove 0 stock it's so slopped on the right...
Yes. Edit. Checked Black Box GBRL settings and nothing has change. So it isn't that.
I set the XYZ Touch Probe Plus at the left front corner of the spoil board a do a xyz probe with a 1/4 end mill. Then put in the spindle a...
So I went to Face a new spoil board and set it to 1mm or 1/32in and it removed 0.115in or about 3mm I even ran it with 0 stock to remove and it...
When I post process to create the g code the last 3 code blocks are not the same as the first 6.