I’m using the x32 black box, and the xyz touch probe plus. Everything is working fine untill I run the automatic probe. I follow the instructions and get it in place then hit confirm and probe. It will move over and probe z. The green light comes on and that’s it. In the control software it shows the job still running. It just sits there not moving on to x,y. I’ve checked the wiring and the troubleshooting tab to make sure it’s making contact and it is. Not seeing errors or anything. Any ideas?
OK, so we've located the bug in Bug: Probe queue stuck · Issue #277 · OpenBuilds/OpenBuilds-CONTROL and have fixed it in a Firmware update: 1) Download CONTROL V1.0.339 (Must be on the latest version of CONTROL) 2) Then follow docs:blackbox-x32:firmware [OpenBuilds Documentation] to update the firmware on your BlackBox X32 3) After updating, try Probing again Let us know if you get stuck on any step
Ok finally had time to try this, and am running into another issue. Per intruction, download new control, and followed update intructions. and receive this error. I've tried different usb cables, moved them far away from any power cables to no avail. Also im on a 2020 Macbook Pro if that matters at all. Any suggestion is greatly appreciated. Code: [15:19:41] [ 3D Viewer ] WebGL Support found! success: this application will work optimally on this device! [15:19:42] [ websocket ] Bidirectional Websocket Interface Started Succesfully [15:19:55] [ connect ] PORT INFO: Port is now open: /dev/tty.usbserial-AB0PMV0D - Attempting to detect Firmware [15:19:55] [ connect ] Checking for firmware on /dev/tty.usbserial-AB0PMV0D [15:19:55] [ connect ] Detecting Firmware: Method 1 (Autoreset) [15:19:55] [ ] ok [15:19:56] [ connect ] Detecting Firmware: Method 2 (Ctrl+X) [15:19:56] [ ] GrblHAL 1.1f ['$' or '$HELP' for help] [15:19:58] [ $$ ] $0=10.0 ;Step pulse time, microseconds [15:19:58] [ $$ ] $1=255 ;Step idle delay, milliseconds [15:19:58] [ $$ ] $2=0 ;Step pulse invert, mask [15:19:58] [ $$ ] $3=2 ;Step direction invert, mask [15:19:58] [ $$ ] $4=0 ;Invert step enable pin, boolean [15:19:58] [ $$ ] $5=7 ;Invert limit pins, boolean/mask [15:19:58] [ $$ ] $6=1 ;Invert probe pin, boolean [15:19:58] [ $$ ] $7=0 ;Disable spindle with 0 speed, boolean [15:19:58] [ $$ ] $8=0 ;Ganged axes direction invert as bitfield [15:19:58] [ $$ ] $10=511 ;Status report options, mask [15:19:58] [ $$ ] $11=0.020 ;Junction deviation, millimeters [15:19:58] [ $$ ] $12=0.002 ;Arc tolerance, millimeters [15:19:58] [ $$ ] $13=0 ;Report in inches, boolean [15:19:58] [ $$ ] $14=0 ;Limit pins invert, mask [15:19:58] [ $$ ] $15=0 ;Coolant pins invert, mask [15:19:58] [ $$ ] $16=0 ;Spindle pins invert, mask [15:19:58] [ $$ ] $17=0 ;Control pins pullup disable, mask [15:19:58] [ $$ ] $18=0 ;Limit pins pullup disable, mask [15:19:58] [ $$ ] $19=0 ;Probe pin pullup disable, boolean [15:19:58] [ $$ ] $20=0 ;Soft limits enable, boolean [15:19:58] [ $$ ] $21=1 ;Hard limits enable, boolean [15:19:58] [ $$ ] $22=1 ;Homing cycle enable, boolean (Grbl) / mask (GrblHAL) [15:19:58] [ $$ ] $23=3 ;Homing direction invert, mask [15:19:58] [ $$ ] $24=50.0 ;Homing locate feed rate, mm/min [15:19:58] [ $$ ] $25=1000.0 ;Homing search seek rate, mm/min [15:19:58] [ $$ ] $26=250 ;Homing switch debounce delay, milliseconds [15:19:58] [ $$ ] $27=5.000 ;Homing switch pull-off distance, millimeters [15:19:58] [ $$ ] $28=0.100 ;G73 retract distance, in mm [15:19:58] [ $$ ] $29=0.0 ;Step pulse delay (ms) [15:19:58] [ $$ ] $30=1000.000 ;Maximum spindle speed, RPM [15:19:58] [ $$ ] $31=0.000 ;Minimum spindle speed, RPM [15:19:58] [ $$ ] $32=0 ;Laser-mode enable, boolean [15:19:58] [ $$ ] $33=5000.0 ;Spindle PWM frequency [15:19:58] [ $$ ] $34=0.0 ;Spindle off Value [15:19:58] [ $$ ] $35=0.0 ;Spindle min value [15:19:58] [ $$ ] $36=100.0 ;Spindle max value [15:19:58] [ $$ ] $37=0 ;Stepper deenergize mask [15:19:58] [ $$ ] $39=1 ;Enable printable realtime command characters, boolean [15:19:58] [ $$ ] $40=0 ;Apply soft limits for jog commands, boolean [15:19:58] [ $$ ] $43=1 ;Homing passes [15:19:58] [ $$ ] $44=4 ;Homing cycle 1 [15:19:58] [ $$ ] $45=3 ;Homing cycle 2 [15:19:58] [ $$ ] $46=0 ;Homing cycle 3 [15:19:58] [ $$ ] $62=0 ;Sleep Enable [15:19:58] [ $$ ] $63=2 ;Feed Hold Actions [15:19:58] [ $$ ] $64=0 ;Force Init Alarm [15:19:58] [ $$ ] $65=0 ;Require homing sequence to be executed at startup [15:19:58] [ $$ ] $70=7 ;Network Services [15:19:58] [ $$ ] $73=1 ;Wifi Mode [15:19:58] [ $$ ] $74= ;Wifi network SSID [15:19:58] [ $$ ] $75= ;Wifi network PSK [15:19:58] [ $$ ] $100=199.100 ;X-axis steps per millimeter [15:19:58] [ $$ ] $101=199.100 ;Y-axis steps per millimeter [15:19:58] [ $$ ] $102=622.050 ;Z-axis steps per millimeter [15:19:58] [ $$ ] $110=2500.000 ;X-axis maximum rate, mm/min [15:19:58] [ $$ ] $111=2500.000 ;Y-axis maximum rate, mm/min [15:19:58] [ $$ ] $112=2500.000 ;Z-axis maximum rate, mm/min [15:19:58] [ $$ ] $120=150.000 ;X-axis acceleration, mm/sec^2 [15:19:58] [ $$ ] $121=150.000 ;Y-axis acceleration, mm/sec^2 [15:19:58] [ $$ ] $122=150.000 ;Z-axis acceleration, mm/sec^2 [15:19:58] [ $$ ] $130=810.000 ;X-axis maximum travel, millimeters [15:19:58] [ $$ ] $131=730.000 ;Y-axis maximum travel, millimeters [15:19:58] [ $$ ] $132=90.000 ;Z-axis maximum travel, millimeters [15:19:58] [ $$ ] $300=Grbl ;Hostname [15:19:58] [ $$ ] $302=192.168.5.1 ;IP Address [15:19:58] [ $$ ] $303=192.168.5.1 ;Gateway [15:19:58] [ $$ ] $304=255.255.255.0 ;Netmask [15:19:58] [ $$ ] $305=23 ;Telnet Port [15:19:58] [ $$ ] $306=80 ;HTTP Port [15:19:58] [ $$ ] $307=81 ;Websocket Port [15:19:58] [ $$ ] $341=0 ;Tool Change Mode [15:19:58] [ $$ ] $342=30.0 ;Tool Change probing distance [15:19:58] [ $$ ] $343=25.0 ;Tool Change Locate Feed rate [15:19:58] [ $$ ] $344=200.0 ;Tool Change Search Seek rate [15:19:58] [ $$ ] $345=100.0 ;Tool Change Probe Pull Off rate [15:19:58] [ $$ ] $370=0 ;Invert I/O Port Inputs (mask) [15:19:58] [ $$ ] $384=0 ;Disable G92 Persistence [15:19:58] [ $$ ] ok [15:19:58] [ $I ] [VER:1.1f.20220325:leadmachine1010] [15:19:58] [ $I ] [OPT:VNSL2,35,1024,3,0] [15:19:58] [ $I ] [NEWOPT:ENUMS,RT+,HOME,TC,SED,WIFI,SD] [15:19:58] [ $I ] [FIRMWARE:grblHAL] [15:19:58] [ $I ] [NVS STORAGE:*FLASH] [15:19:58] [ $I ] [DRIVER:ESP32] [15:19:58] [ $I ] [DRIVER VERSION:220327] [15:19:58] [ $I ] [DRIVER OPTIONS:v4.3.2-555-gb4ef1b80a2-dirty] [15:19:58] [ $I ] [BOARD:BlackBox X32] [15:19:58] [ $I ] [AUX IO:1,0,0,0] [15:19:58] [ $I ] [WIFI MAC:94:B5:55:35:89:38] [15:19:58] [ $I ] [IP:0.0.0.0] [15:19:58] [ $I ] [PLUGIN:SDCARD v1.05] [15:19:58] [ $I ] [PLUGIN:ESP32 WebUI v0.03] [15:19:58] [ $I ] ok [15:19:58] [ $G ] [GC:G0 G54 G17 G21 G90 G94 G49 G98 G50 M5 M9 T0 F0 S0.] [15:19:58] [ $G ] ok [15:19:59] [ connect ] Firmware Detected: grbl version 1.1f on /dev/tty.usbserial-AB0PMV0D [15:20:15] [ Firmware Upgrade ] [Starting...] [15:20:15] [ disconnect ] PORT INFO: Port closed [15:20:15] [ Firmware Upgrade ] env: python: No such file or directory [15:20:15] [ Firmware Upgrade ] [exit:127] [15:20:15] [ Firmware Upgrade ] Firmware Update FAILED! Please review the logs above, or try again
Any chance you have a Windows machine nearby? If not, the error complains Python is not installed. ESPtool uses python.