I just completed my Lead 1010 build and ran some initial tests (hello world example) yesterday and all seemed good. I tried again today and I ran into an issue. My x-axis motor is now much louder then the others and when I press the jog button (X+, 10mm increments) it reverses direction if I press the button back-to-back quickly. If I use continuous jog it seems to work but if I release the button and press it quickly I have the same issue and it will reverse directions. I'm not sure what is going on as this is my first CNC. Any help troubleshooting this issue would be greatly appreciated.